That Wednesday shift where nothing went right on the Haas VF-3
I had a day last month that still bugs me when I think about it. I was running a production job on our Haas VF-3, and the first part came out with a bad surface finish on the chamfer. Turned out the insert had chipped, so I swapped it and re-ran the part. Then the coolant pump started making this grinding noise about an hour later, and I had to stop and clean the filter in the tank. After that was fixed, the probe failed to set the work offset on the next part, so I lost another 20 minutes troubleshooting. Three things went wrong in one 6 hour shift, and I only got 12 good parts out of the 30 I needed. Has anyone else had a run of bad luck like that on a simple job?